Imagine the underside of the slide with barrel, recoil spring, and recoil spring guide rod removed.
Holding the slide barrel end down with the bottom facing me, I noticed that the rear base of the bolt (below the safety at this perspective) had strike marks on only one side from the hammer dragging on it as the slide was blown rearward during the extraction and ejection stages. However, this mild wear was uneven. There was far more at the distal end, tapering off before it reached the proximal end, indicating: 1) the hammer was dragging unevenly on one side of the bolt, and 2) the slide was not fully reaching the rear. The latter would seem to explain why this pistol was having so many problems with extraction and ejection. Moreover, a slow return would not seat the new round fully, causing the misfires.
I put a micrometer on the slide, comparing the measurements of the right and left sides of the bolt. There was a difference. To be sure, I ran a laser level across it.
I marked the high spot with a Sharpie. I used a dremel tool with pen accessory and bits for the work. Those, in turn, were a mild stone, a wire, and afterwards jewelers rouge on a cloth wheel to polish the steel until the laser beam point was circular on the wall next to my bench.
As I said, that did the trick. Fired without problems the same ammo that had not worked an hour before (Winchester).
Thanks for the advice on the sight. I am leaning towards a metal sight that I can screw in from the inside and Loctite into place. I don't know what that is yet. If there isn't anything commercially available, I expect that I will modify an iron sight that fits well enough, then braze it in. The original sight grouped 3" low at 7 yards for me. My wife relies upon the laser in any case. She'd be just as happy with no sights.
MFF JM